I thought, again, that maybe I should revive this stupid blog, and I found that I'd already written most of an entry and left it as a draft. I didn't publish it, because I had a list of other stuff I thought I should talk about and I was only halfway through the list. Well, looking at the list now, most of what was left looks boring, or unimportant, or I've forgotten the details now. All of which fits the theme of this blog pretty well, but I think I'm just going to punt on all of those things, except for one, which will possibly go into a future entry.
Anyway, my last entry was a first effort at getting caught up on all the stuff that happened after I got the car home from the body shop for the second/final time. I got maybe halfway through all that stuff, and then just decided to punt and publish, so now I need to get through the other half. As the character Jeff Jordan says to the character Pete Aron in my favorite racing movie (Grand Prix), "Go another halfway!!!"
I talked in a previous post about how I had problems with the clutch pedal stop latching onto a bolt on the firewall when the clutch pedal was depressed, which made the car very awkward to drive. I tried to fix that by modifying the clutch pedal stop, but I still had issues with the clutch. Sometimes it just felt kind of "creaky," like there was some excess friction in the master cylinder. It didn't seem right, and I eventually happened to hear about a clutch arrangement from another company that I thought might work better. I had originally gotten a master cylinder from McLeod, because that was the company that I got all my other clutch stuff from. But, they didn't have a master cylinder that was meant for my car, so I'd tried to make something else work. Eventually I heard about a "universal" master cylinder from American Powertrain, and I saw some video of how it worked, and I thought it looked like it would be an improvement.
I think the big problem with the other master cylinder I tried to use was that when it was bolted to the firewall, it was not parallel with the pushrod that connected it to the clutch pedal. I got it pretty close, but apparently "pretty close" was not close enough. This resulted in side-forces on the master cylinder piston, which resulted in the "creaky" operation.
With the American Powertrain universal master cylinder, it uses a mounting bracket that is hinged so that the angle can be adjusted in order to make it parallel to the pushrod. The photo below shows the American Powertrain master cylinder mounted in the Impala, and you can see the hinged mounting bracket. After the position has been adjusted, the bracket is locked down so that it won't move out of the correct position.
So that sorted out the clutch pretty well.
Another thing that needed finishing was installing the oxygen sensors. I talked in an earlier entry about the work I did to install the display in the dashboard, but now that everything was together and the exhaust pipes were under the car, I still needed to install the actual sensors, and finish the wiring between the sensors and the display.
There's three wires for each oxygen sensor, plus a ground for each, so with two oxygen sensors that makes eight wires to run through the firewall. I didn't want to just put another hole in the wall and run wires through it, so I got a twelve-pin bulkhead connector from McMaster-Carr. The photo below shows the connector, on the engine side of the firewall.
One nice thing about this connector is that the terminals install from the back side of the plugs, which makes it relatively easy to install new wires if you want to add more later. If something else needs to be wired through the firewall, just unscrew the nut that clamps the gland down on the wires, crimp a terminal on the new wire, stick it through and push it in until it clicks, then clamp the gland back down on all the wires.
Once the oxygen sensors were working, I had some feedback on the air-fuel ratio. It showed that the engine was running pretty rich, which was no surprise. Carburetors usually come out of the box running pretty rich, because it's better to be on the rich side than the lean side, and they don't know all the particulars of your engine, or where you plan to run it, etc., etc. I decided to lean it out by going two sizes smaller on the primary jets, for starters. That seemed to show some small improvement, but it still appeared to be pretty rich. As it turned out, though, for those couple of months in the Texas "winter," when the temperature might be in the 40s in the morning and the air is dense, it runs about where I would want it to be all the time. I wouldn't want to go much leaner than that, so I guess by letting it run a little rich for most of the year, it ensures that I won't be too lean in the winter months.
After I had been driving the car a little while, I stopped to get gas one day, and when I twisted the gas cap to remove it, it kind of popped off into my hand as soon as it was unlatched, and there was a "PUFF" of gas vapor in my face. Well that's odd.... I had gone to some trouble to keep the factory gas tank vent line in place, because I didn't want to disturb its grommet where it passes through the floor of the trunk. The vent line connects to the front of the gas tank, at the top, and then runs through a hole, up into the trunk, then loops back down, passes out through the same hole, and has an open end to vent to atmosphere. The purpose of running up into the trunk is just to get the high point of the vent line high enough so that gas won't slosh out of it. Because the line passes through the same hole twice, it takes a special grommet with two holes in it. I didn't know where I could get a replacement grommet, and I was afraid that it was probably so old and dried out that it would crumble if I tried to remove the old line and put a new line through it. Well, one thing I never thought to do at the time was to verify whether or not the vent line was open. Sure enough, it seemed to be plugged solid.
I was able to get a stainless steel reproduction vent line, and even had a few different options for where to get it. I think I tried Year One first, because they seem to have the best stuff, in terms of matching the original parts and fitting up correctly. But, they wanted to charge me something ridiculous for shipping. The part was something like $40, and I hate to even say this because it sounds too ridiculous to be true, but I think they were going to charge something like $100 for shipping, just because the line is an "oversize" shape. It only weighs a couple pounds, but they had this huge additional shipping charge because of its size and shape. Anyway, I ended up looking around, and eventually found that Classic Industries had the line for $35, and I was able to order it when they had a deal going for free shipping. Free, by my math, is a better deal than $100.
The photo below shows how the line loops up and over in the trunk. It seemed to be a little longer than the original, and its highest point was right up by the body work. It was actually right against the steel. I was worried it would vibrate and cause a rattle when driving, so I decided to get a P-clip with a rubber sleeve on it, and I drilled a hole to bolt that clip to the body work, thereby stopping the line from rattling.

Once I was able to start driving the car, I noticed that it had a slight vibration at highway speed. It was hard to say where it seemed to be coming from, but it seemed to be road-speed-dependent, so I thought it was probably something rotating, and something down-system of the transmission. That pretty much left the driveshaft, the rear end assembly, and the wheels.
Out of all that, the wheels and the driveshaft seemed the most likely. My first thought was that maybe the pinion angle had changed since I first set it. Once the car is driven a few times, it is not uncommon for the suspension to settle, and maybe that had affected the pinion angle? Coincidentally, around this time I happened to catch an episode of one of these custom-car-shop-reality-shows, and they showed a customer bringing his car back with a vibration after he'd had it for a month or two, and the fix ended up being correcting the pinion angle. Now I was onto something!
I re-checked the pinion angle, and it was off a bit. I had used a free app from Tremec that lets you check the angle of the pinion, the angle of the transmission, and the angle of the driveshaft using your phone as an angle finder, and then it tells you whether you are within the allowable limits. The first time I did it, it seemed like it was repeatable, or at least predictable enough that when I made an adjustment and re-checked, I could predictably move the pinion to the correct position. But now when I went back to re-check it, it did not seem to be repeatable or predictable. So this time I used a mechanical angle finder to take the measurements, calculated the result myself, and adjusted it until it was back in spec. That made me feel better about the pinion angle, but it did not fix the vibration.
I had noticed by this point, also, that there were very slow oil drips from the seals at the end output of the transmission and the input of the differential. I put together a theory that the vibration might be caused by the driveshaft being out of balance, and that the resulting wobble of the driveshaft was causing the seals to leak, as well. I tried to research online a bit and see if anyone else had ever had a similar problem, but didn't come up with anything helpful.
I had ordered the driveshaft online from a place in New York (state), because I had read something about the importance of getting your driveshaft from a place that knows how to properly balance it, and because they bragged a lot on their website about how they balance their driveshafts better than anybody. What they said seemed to make sense (they went into more detail than just saying they were better than anybody), and they asked for a whole page full of measurements when you place your order, which made me feel like they must know what they're doing. So it was frustrating now to talk myself into thinking that the shaft wasn't balanced properly after all. Still, if nothing else, they did send me a free t-shirt with the driveshaft (or maybe a free driveshaft with a very expensive t-shirt?), and it became one of my absolute favorite t-shirts, so that was certainly worth it.
By the time that I was second-guessing their work, however, I had now become aware of a driveshaft shop in town that has a very good reputation, so I decided to take my driveshaft to them and have it checked. They're not open on weekends or evenings, so this required taking a day off from work. When I went in there and explained what I wanted and why, one of the guys told me that he would recommend replacing the seals in the transmission and the differential and see if they still leak, because that would be cheaper than having them balance the driveshaft. But, at that point I had already taken the day off and removed the driveshaft and driven it across town, and I just wanted to get it checked and get that over with. So eventually they agreed to just check the blankety-blank driveshaft.
After running the check, one of the guys let me come back and see the test rig, and he showed me the results. He said he could add one small weight and it might technically make it better, but based on what the rig was showing, he would not expect someone in the car to be able to feel any vibration from the very small imbalance that he had found. By this time I figured I was wasting my time, but also I was already there, and we had come this far, so if we can make it a little better, let's do that. So he added the small weight, and then I paid and took my driveshaft home.
(I was favorably impressed by their shop and their service, and later I bought a new driveshaft from them for my C10 when I repowered it with a big block. I never did, however, get any t-shirt out of that deal.)
They were right, the driveshaft did not make any difference in the highway-speed vibration. I kind of lived with it as it was, and it wasn't real bad. After a while, if I recall correctly, it seemed like it was most noticeable when I had first gotten up to highway speed, and then it would smooth out a bit. As I made it a point to pay more attention to it, and tried to figure out where it was coming from, eventually one day I decided that it felt like it was coming from the right front wheel. I'm not sure how to describe how I thought I could tell that, it just felt that way.
To test the idea, I swapped the right side tires front-to-back, and sure enough, the next time I took it on the highway it felt like the vibration was at the right rear. I pulled off just that wheel and took it to a local Firestone shop to have the balance checked. They confirmed that it was out of balance, but said they'd probably need to apply balance weights both inboard and outboard in order to correct it, and was that OK?
What?
So, the tires were originally mounted at the shop that did the powdercoating on the rims. I dropped off rims and tires, they powdercoated the rims and mounted the tires. Powdercoating costs more than painting the rims, but it results in a more durable finish. I wanted a durable finish because I didn't want my steel rims to start rusting immediately. But a lot of people who get rims powdercoated are building show cars that they just want a high-quality finish that will look good. A lot of those people will also choose, I learned, to have the wheels balanced only with inboard balance weights. In that way, there are no weights visible on the outboard side of the wheel, which presents a cleaner look for show cars. And, since many of these people will only drive their cars to and from shows, or possibly even just on and off of trailers, they don't really care if they sacrifice the quality of the balance job.
This was all news to me, but my assumption after the fact is that the powdercoat shop just assumed that I didn't want outboard balance weights, or maybe they don't even carry those type of weights. Anyway, they never asked what I wanted, and they only used inboard balance weights. So now I told the guys at the Firestone shop, heck yeah, balance weights everywhere, balance weights all around, whatever it takes. So they added some outboard balance weights, and when I got the wheel back on the car, and up to highway speed ... smooth as glass. Fantastic.
The next item is a relatively minor feature that most people will never even notice, but it's one of my absolute favorite things I did on the car.
I have struggled to find good joyriding roads in the San Antonio area. Growing up in the Chicago suburbs, there were lots of nice forest preserves around, with roads that wind past ponds, through densely wooded areas. They were relatively short runs, but it also didn't take long to get to them, and it was satisfying to just go out and drive around a little bit. Texas, on the other hand, is a barren wasteland where nothing will grow. San Antonio is, however, on the edge of what's reverentially known as "The Texas Hill Country." The Texas Hill Country has a lot of nice winding roads through hills, even if there are no ponds or forests to be found. It takes a drive up the interstate just to get out away from the city first, though, so it's not really as convenient as being surrounded by forest preserves within the suburban area. Oh, well.
Anyway ... one night I decided to go out for a joyride through The Texas Hill Country. I just took I-10 up to 46, and then followed 46 back to 16, and took 16 back to 410, and then 410 home. Out on 46 after dark, though, I had the headlights on, of course, and I was flipping the high beams on and off, depending on whether or not there was oncoming traffic in sight. As I detailed in an earlier entry, I put in a row of toggle switches on the left side of the dash, and I put all of the headlight switch functions on those toggle switches. Well now, driving around in the dark in The Texas Hill Country, I suddenly realized that I could not see any of those switches in the dark. So there was a lot of fumbling around for the high beam switch every time I needed to cut them on or off.
I thought about it a little bit, and developed a vague idea for a way to light the switches, although I wasn't really feeling confident that I'd be able to make it a reality. But I started lining up parts to try something. I started by ordering a strip of LEDs off of Amazon. The photo below shows the strip of 15 LEDs. As I recall, the LEDs were wired in groups of three, so it was five groups of three, with the threes in series and the groups in parallel. So, if you cut off one LED, only twelve would light, and the two on the end that you cut would no longer work. It was a little longer than I needed, so I cut off the last group of three and made it a strip of 12 LEDs. When I tested the LEDs, they seemed really bright, so I also got some resistors and wired them into the 12V wire to drop the voltage and dim the LEDs. You can see the resistors in the photo below, too.






































